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Co-pilot’s bravery helped save lives, inquiry into fatal helicopter crash told

Four people died in the Super Puma L2 ditching off Shetland in 2013, while 14 survived.

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Shetland helicopter crash

The actions of a “brave” co-pilot who armed the floats of a helicopter in the moments before it plunged into the sea saved lives, an inquiry into the fatal crash has heard.

Captain Alan Findlay, a search and rescue helicopter pilot, said Alan Bell showed “great presence of mind” when he triggered the devices that prevented it from sinking.

Two crew members and 12 passengers on the Super Puma L2 survived when it ditched on its approach to Sumburgh Airport in Shetland at 6.17pm on August 23 2013.

But Sarah Darnley, 45, from Elgin, Moray; Gary McCrossan, 59, from Inverness; Duncan Munro, 46, from Bishop Auckland, County Durham, and George Allison, 57, from Winchester, Hampshire, died.

Shetland helicopter crash
Victims Duncan Munro, George Allison, Gary McCrossan and Sarah Darnley (Police Scotland/PA)

Captain Findlay, who worked at helicopter firm CHC at the time of the crash, praised Mr Bell’s actions before the impact.

He told the fatal accident inquiry (FAI): “It saved people’s lives. By arming the floats it then meant that they would automatically deploy on water contact.

“If the floats were not armed and the aircraft hit the water then the floats would not have deployed automatically.”

Captain Findlay, a witness for the Crown, prepared a report on the crash with three other pilot experts for the FAI, which is being held virtually due to coronavirus measures.

Commenting on Mr Bell’s actions, he said: “It had a very significant effect on the survivability of the crash.

“We all felt it was noteworthy that in a very short period of time realising that things were going very badly wrong he was able to do that very important action, it showed a good presence of mind.”

He added: “That was by far the most important thing that he could to do affect and alter the circumstances that he found himself in.”

Survivor Samuel Bull took his own life in London in 2017, which sheriff principal Derek Pyle said was “directly caused” by the crash.

An AAIB report published in 2016 found the pilots failed to properly monitor the flight instruments and failed to notice their speed was decreasing until it was too late to avoid the Super Puma plunging into the sea.

Captain Findlay said while both Captain Martin Miglans – who was acting as pilot flying and the co-pilot, who was acting as pilot non-flying (PNF) – had shared responsibility for monitoring the instruments, the PNF also had many other duties such as answering radio calls and looking out of the window to check visual references.

David Adams, representing the Darnley family, said the helicopter dropped from a speed of 80 knots to 35 knots over 30 seconds and asked who had responsibility for monitoring the speedometer.

Shetland helicopter crash
The wreckage of the Super Puma L2 helicopter in 2013 (Danny Lawson/PA)

Captain Findlay, who was giving evidence from Australia, said the pilot flying had 100% responsibility for looking at the instrument while the PNF would look whenever he was able to look amid his other responsibilities.

He said it was “inexplicable” the captain did not notice the airspeed dropping and suggested it could either be because he had a medical episode that meant he was looking but not seeing or that he was simply not looking.

Captain Findlay also said the autopilot mode chosen for the approach, which did not use all the automation available, was a “poor choice”.

The helicopter was being flown in three axes with vertical speed (V/S) mode as opposed to four axes mode which used all the automation.

He said using the three axes mode is not prohibited by the standard operations manual but he was shocked to hear many North Sea pilots at the time used it as it makes the approach “much more unstable and difficult”.

Captain Findlay said at the time many pilots in the area were used to operating in three axes and there was a “mistrust” of four axes, which might explain why pilots decided to choose the former.

He also told the FAI it was a “major omission” by Captain Miglans not to mention what mode of autopilot he was choosing in his briefing to the co-pilot as that would have highlighted the importance of paying attention to the air speed.

A statement of agreed evidence read at the start of the inquiry confirmed that no mechanical fault was discovered with the helicopter, which was returning from the Borgsten Dolphin support vessel to Sumburgh Airport when it ditched.

The inquiry continues.

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